One thing to remember here is that the intent of the Nov 3 experiment was to record internal temperatures = to see if high enough temperatures would be produced, and maintained, to allow for potential iron smelting.
In this, the effort can be seen as a success. Thanks to instrumentation provided by Neil Peterson, there was much better temperature data records than normally generated.
As detailed in the previous description, the addition of ore did not exactly follow our well proven 'best practice' :
- There was no initial addition of iron rich slag, which has proven to quickly establish a working slag bowl system, increasing both yield and bloom density. (1)
- The amount of ore added was on the small end. In the past it has been found that the first ore is primarily creating that same working slag bowl system, with the later amounts mainly contributing to iron mass on to the bloom. (2)
- The quality of the bulk of ore used was questionable, with past uses of the same lot of material seen to result in low yields at best. (3)
The following morning (so plus 16 hours), it was found that the charcoal had all burned away inside the furnace, but the exterior base was still warm to the touch. In actual fact, it would be another three weeks until the furnace was actually opened...
Nov. 3 - after cutting |
View of interior, showing tuyeres with mass below |
Judging from the heat effects, it appeared that the placement of the tuyeres was in fact quite effective in concentrating the heat into the centre of the furnace. (Rather than washing back on to the walls and erroding them, which likely would have been the case with a shorter insertion length.) (5)
Neil Peterson undertook the excavation of the furnace base. Recording the process was done through an extensive series of scaled photographs he made (only a few reproduced here).
Walls removed to about tuyere level (image by Neil Peterson) |
Detail of lower left, before 'cleaning' (image by Neil Peterson) |
There was no clear bloom mass in evidence. The top surface was roughly bowl shaped, higher under each of the tuyeres and depressed to the centre. The material had a 'crumbly' surface texture, looking like reduced but only partially sintered iron with a lot of slag included. Unfortunately no exact measurement of the depth of this surface below tuyere level was made, but looking at the images, it appears to be about 6 - 8 cm lower to the centre.
One of the tuyeres removed (image by Neil Peterson) |
Another tuyere, image rotated to 'square' (image by Neil Peterson) |
After the tuyeres were removed, the remaining wall material was cleared down to expose the slag mass.
The slag mass exposed, surface cleaned |
In the image above, one further course of clay additions was been removed from the left side. You can clearly see the difference in heat effect. The upper level (closer to tuyere blast and thus the full furnace heat) shows slag attached to its inner surface. Clay shows sintering (white) from the inside outwards, carbonization of the horse manure organics, then dry baked clay to the exterior. In comparison, the next course down (just above the brick plinth) is only baked dry clay. The height difference between these layers is no more than 10 cm.
Mass exposed, side view - rotated to level (image by Neil Peterson) |
Slag mass removed, the right edge broke clear - image altered to place 'neck' at horizontal (image by Neil Peterson) |
Later in the day, the large mass was broken open (we still had hopes there might be an iron bloom inside...). The mass broke apart into several large chunks, and along the central 'neck' line.
Part of the lower, slag block (top uppermost) |
Upper mass - bottom side (against lower slag) |
Upper mass - side towards tuyeres |
next posting - Conclusions...
Prepared with some observation checking help from Neil Peterson.
1) What I call the 'Nissen Method'. This was demonstrated, to great result, by Danish experimenter Michael Nissen at the 2016 Pruszkowski Festival of Archaeology. In brief,3 - 5 kg of crushed iron rich tap slag is added as the first series of charges. This material will immediately form the effective slag bowl, so as ore is added after, it goes directly to iron bloom formation. Typically this method has been found to increase effective yields by about 10% (overall).
2) In relation to above. In the past it has been found (depending on ore type) that about the first 8 kg of ore goes into forming the working slag bowl system. Material added after that is generating bloom mass. This is especially true of those ore charges added to the end of the sequence. Our normal process here is to use roughly 30 kg of ore, with the expectation (with our DD analogs) of a bloom return of 20 - 25 % / 3 - 5 kg. Both raw size and yield % will sharply rise with larger ore additions. Remember that the overall intent of the various experimental series is primarily testing various furnace types and detailed builds - not production per se.
3) This specific ore lot was found to be generally 'poor' - with considerable slag, small blooms, and low yields, from earlier uses : Nov 5, 2006 / June 9, 2007 / Oct 27, 2007
4) Nov. 3 - 'Gromps' smelt. Report still pending.
One factor is that Neil proceeded to 'excavate' the MoAF-I furnace, while I was guiding a second team in preparing for a second experimental smelt. Both furnaces under the smelting area at Wareham, about 1 metre apart!
5) Through past experience, using higher volume air (bellows or electric blower), it has been found the 'sweet spot' for the tuyere tip is about 5 cm proud of the interior wall. When using mild steel pipe, these almost always will burn back to maintain that '+5 from wall' distance.
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